Monday 19 October 2020

Dillon Primer Early Warning System - Rebuild and Modification

The Dillon Primer Early Warning System is a simple but robust product.  However if you leave a battery in there it will corrode all of the internal electronics.  This was the case with two units I was given to fix.  Internally one of the batteries was in two pieces, the acid and acidic fumes had eaten away the copper wire, destroyed the buzzer and was all over the micro switch and most likely also inside it.

On stripping out the electrical parts I found the bottom battery spring showed no signs of corrosion at all.  The plastic case was covered in muck but was easily cleaned after a good soaking in sodium bicarbonate to neutralize the acid.

The electric are very simple.  a micro switch where the common contact is used for the battery contact.  There are two contacts on the side the top one is cut, which the normally closed contact.  The bottom contact is normally open which is connected to a wire to the buzzer.  From the buzzer runs a second wire to the spring which is the contact for the other end of the battery.

When talking about the repair I also discussed what else could be done to upgrade the product. Basically we came up with 3 things.
  1. A louder buzzer : as older long term shooters tend to be a bit deaf
  2. A bright red warning light : again due to deafness
  3. A way to still run it off of a 1.5 Volt AAA battery

This particular unit had an electro-mechanical buzzer that was totally corroded.  I stripped out the insides but retained the plastic case to hold the Piezo buzzer.

It should be noted that most Piezo speakers will NOT make any noise with out and external oscillator.  When purchasing one ensure it has a BUILT IN OSCILLATOR.

It also turns out that the Piezo buzzer in the new Dillon products is already at the 85dB limit.  Going louder than that will just worsen you hearing further.

I bought some LED holders to hold the LED light as you can see from this picture when mounted it looks pretty swish.  

 

 

 

 

 

The second picture shows the stripped down components with the LED in place.

To add a LED light it was easier to source 3.3 volt parts.  However as the device can only take a single AAA battery at 1.5 volts I needed a boost converter.

 
BOM
 

1 x 3.3 Volt boost converter          -       Pololu 3.3V Step-Up Voltage Regulator U1V10F3 - $7 AUD

1 x 3 Volt high brightness LED    -      TLDR4900 LED, 3MM, RED - $2.96AUD for 5

1 x 3mm LED holder                    -    A104700BLACK LED HOLDER, T1, PK5 - $15.61 for 5

1 x 3.3 Volt PiezoIndicator           -    Continuous tone magnetic 3Vdc 85dB HS code 85318000 - $13.85 for 5

1 x 150 Ohm resistor                        This is for the LED, to stop it drawing too much current.

1 x Double sided tape                    - 

1 x Spool wire wrap wire               -

 
As you can see space was pretty tight but the end result had a nice professional finish. 
 
 





 


Wednesday 14 October 2020

Sony WH-1000XM3 - Replacing the USB-C connector

I've been fairly consistantly doing a lot of soldering over the last few years, both surface mount and through hole.  Every now and then I accept "easy" jobs from my friends.  I've fixed buttons on car key fobs, micro usb connectors and now the USB-C connector on Sony WH-1000XM3 head phones.

This has probably been the first item where I've not been able to get to the pins to solder them on.  So lets have a look at what is involved.

Deconstruction

The headphones are really nicely put together and very repairable, something other manufacturers should take note of.


Using a spudger start at the side and make your way around to remove the foam ear piece.



Luckily there are only screws and a bit of tape holding it together.  Remove the first flexible connector.


Remove the plastic cover to expose the USB-C connector


Remove the second flexible connector and the small PCB. Look at that mess of crushed pins.


Using a Hot Air tool remove the connector.  You'll notice I've left the solder on the pads.
 
 

Which part is this?

 
        

Now that I had the part off it was off to RS-Components to play match the foot print.  With some digital calipers in hand and data sheets on the screen I managed to find a good match.

 

Reconstruction


 
I left the solder on the pads on purpose so I could reflow it with my Quick 861DW.
Carefully tin the small connector pins.
Place back on the PCB.
Now use your Hot air tool to relflow it with a little downward pressure. Keep the air down quite low. I had it on 40 l/min
 

Make sure you secure it properly as you do not want it to break off.

 
It lives . . . actually I tested it quite a bit before putting it back together.

Thursday 7 May 2020

Abandon ship . . .

Well not really . . . 

I've started focussing on just my retro projects so if you're interested in on old Commodore related stuff that I'm working on head off to https://8bitshardway.blogspot.com/

Hopefully I can jam some interesting CPLD FPGA stuff in there :-)